I started with some 20mm Delrin bar
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I then turned this down at one end to allow me to tap it to 1/4" BSP at 19 turns per inch with is a standard pneumatic fitting in the UK.
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I then applied a thread to it with a die that my Grandfather left me.
I held the die by hand with the work piece in the lathe chuck. I turned the chuck with the chuck key.
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Ironically, I was applying a British Standard Pipe thread with a die that was made in the USA.
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I then put a chamfer on the thread to ease starting the thread
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The next stage was to drill a 2.5mm hole through the nozzle
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And added a taper to reduce the internal diameter from 1/4" to 2.5mm
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I then added an external taper using the lathe cross slide at an angle
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Here is the finished nozzle
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Here is a video of the solenoid valve in use
The trigger is very responsive but as I experienced last time, the range is greatly reduced. I got about 28 geet out of this test. The problem is that the solenoid valve has a restricted inlet port and this is where the problem lies.
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I've decided to give up on solenoid valves. They are OK with air but water is too viscous. Ball valves are the way to go, but automating them could be a pain.
However, I do have some experience with pneumatics, and I have a tank full of compressed air on my back.......Watch this space.
1 comment:
Since, the solenoid valve has small hole through the nozzle of 2.5mm, it create more pressure. And adding the taper to reduce the internal diameter is a big help.
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